#21
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Re: Decarbonizing 1999 Johnson 175 Carb.
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#22
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Re: Decarbonizing 1999 Johnson 175 Carb.
If you were spinning 5600 before and you're only turning 4600 now (no changes except for the decarb) then you're firing on 5 of your 6 cylinders.
Pull all the plugs and inspect the white ceramic part . . . all of them should be paperbag brown in color. One will be white. That's the one that isn't firing. Replace that one spark plug and/or make sure the coil and plug caps are on tight. Take her for another spin. Oh yeah . . . You probably have to gap your plugs on the OMC motor . . . so make sure that your in spec with the gaps. See the carbon on the ends and the paperbag brown color on the tip. That's good . . . The one that comes out looking brand spanking new (from a nice petroleum high pressure clean). That's the culprit. Fiddle with the wires and the plug cap for that plug and you'll be back up at 5600. |
#23
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Re: Decarbonizing 1999 Johnson 175 Carb.
PeterB, I have not yet checked the compression.
Scott, OMC SS 14 1/2" X 19". Since 1999. Perfect match. BigS, I think you are on to something. That sounds closest. Remember I used original plugs that were used during the decarb, because I didn't THINK that they were that bad. Boat ran flawlessly all day until I wanted to run WOT for a minute or so. After sitting on a sand bar for the last hour, we decided to make 5 minute run back to landing. Upon arrival, overheating alarm. Did not run over 3500 revs. to ramp, and was not overtrimmed. Like 12-15 hours on waterpump. Hope to pull plugs today. Thanks all. Part II. |
#24
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Re: Decarbonizing 1999 Johnson 175 Carb.
Mike, just a thought. Why don't you check your linkage and control cables? Maybe your not getting full throw out of them. Check your timing aswell.
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